|Power Reactor||Event Number: 40876|
|Facility: HOPE CREEK
Region: 1 State: NJ
Unit:  [ ] [ ]
RX Type:  GE-4
NRC Notified By: RITA BRADDICK
HQ OPS Officer: MIKE RIPLEY
|Notification Date: 07/16/2004
Notification Time: 14:10 [ET]
Event Date: 07/16/2004
Event Time: 10:00 [EDT]
Last Update Date: 07/16/2004
|Emergency Class: NON EMERGENCY
10 CFR Section:
50.72(b)(2)(i) - PLANT S/D REQD BY TS
50.72(b)(3)(v)(D) - ACCIDENT MITIGATION
GLENN MEYER (R1)
|Unit||SCRAM Code||RX CRIT||Initial PWR||Initial RX Mode||Current PWR||Current RX Mode|
|1||N||Y||95||Power Operation||95||Power Operation|
|TECHNICAL SPECIFICATION SHUTDOWN/LOSS OF
SINGLE SAFETY FUNCTION
"A Unit shutdown was initiated at 1100 [ET 07/16/04] to comply with Technical Specifications. The High Pressure Coolant Injection (HPCI) System was declared inoperable at 1000 on 7/16/04 due to an inability to demonstrate that it is capable of meeting its design flow and pressure requirements identified during an extent of condition review being conducted in conjunction with an ongoing Safety System Design Inspection. Concurrently, the `D' Emergency Diesel Generator (EDG) was inoperable due to an in-progress surveillance. This rendered the `D' Low Pressure Coolant Injection (LPCI) subsystem and `B' Core Spray subsystem inoperable resulting in entry into Technical Specification 3.0.3 requiring within 1 hour initiating action to place the unit in at least startup within the next 6 hours, hot shutdown within the following 6 hours and cold shutdown within the subsequent 24 hours.
"Power ascension was in progress with reactor power at 95%. Power ascension was suspended. Preparations for power reduction were initiated. Actions were taken to restore the `D' EDG to an operable, standby alignment, which was complete at 1145 rendering `D' LPCI subsystem and `B' Core Spray subsystem operable. Technical Specification 3.0.3 was exited. No power reduction was conducted.
"The HPCI system remains inoperable constituting a condition that could have prevented the fulfillment of a safety function. The investigation is ongoing including a determination of the need for any physical modifications that may be required.
"Prior to the event, the `C' Station Service Water pump, `D' Filtration Recirculation, Ventilation System recirculation fan, and `B' Primary Containment Instrument gas compressor were out of service for scheduled maintenance. There were no personnel injuries as a result of this event.
"The NRC Resident inspector was notified of this event."